Nick
02-27-2007, 03:47 PM
So my 244 is dead. This will be the 2nd redblock I've murdered. Unfortunately this is going to be my official dumbass tbricks moment. Heres the story;
I drove home (Vero Beach, about an hour and a half from Orlando) on Saturday evening after work so I could attend my sisters birthday party on Sunday. So I made it home ok, no problems, ate dinner w/ my mom and then went over to kevin's (boosted) to hang out w/ him for a while. So we got kind of bored and decided to go for a ride in my car. Kevin drove it around a little, then we switched and I got in to drive. I made it to the end of second gear at full boost when I noticed something was wrong. I backed off and noticed while the motor was running on 3 cylinders. I figured I had probably blown an IC pipe off or something, so I pulled into a gas station to have a look. Popped the hood and we heard some horrific top end noise. Checked all the normal stuff, and everything seemed ok. Cranked it up again to try and diagnose the sound and thought it might be a shim that popped out of the bucket. Valve cover off.... nope. Cranked it up again to try and hear. This time, there was a terrible rattling noise, but the motor ran better....... hmmmm... At this point we were thinking valve seat, spring, bent valve; something in the head. Compression check showed 185 on 1, 2, and 3 but only 170 on 4. We drove to Sebastian, ripped the head off his old 245 and got some sleep.
Sunday morning I got up, went and ordered the HG set and we went over to the gas station where the car was. Pulled turbo/mani. Went to pull the intake and then we found it. Kevin reached into the intake port on #4 and pulled this gem out:
http://nickflyman.com/volvo/volvo19/IMG_0144.JPG
Yes, folks, thats 1/2 of a hose clamp. The other half had been chewed into the motor by the valve and was inside the cylinder. The only place I can figure this thing came from is the cold side of the IC. I got it from a garage where it had been sitting for some time under a bunch of crap. I inspected and flushed it out, so it must have been wedged solidly into the bottom. The amazing thing is that it stayed down there for a YEAR. I went to SE5 like this. Countless trips from Vero to Orlando. Strange. So we continue pulling the head off and finally have it removed to find this:
http://nickflyman.com/volvo/volvo19/IMG_0140.JPG
http://nickflyman.com/volvo/volvo19/IMG_0141.JPG
and this:
http://nickflyman.com/volvo/volvo19/IMG_0143.JPG
****.
We rolled the motor over and noticed that there was amazingly, no damage to the cylinder walls. The head was f-'ed and we knew that for a fact. This is the first time the motor had been opened up to my knowledge. There was still faint crosshatching on the cylinder walls (this is a 300+k mile motor!). The inside of the engine, except #4 obviously, was surprisingly in amazing shape. What a shame.
It was decided that I should clean the piston crown w/ emory cloth as best as possible, clean up the wagon head, and throw it all together in hope of just getting me back to Orlando where I can spend the time to do a motor swap.
http://nickflyman.com/volvo/volvo19/IMG_0149.JPG
We reassembled and got it running. Now the amazing thing is, that the motor ran very well. I drove it around Vero some, home that night, over to my sister's thing, and back home. The next morning (yesterday) I depart for Orlando. Fires right up, get on 95, no issues, pull off on 520, no issues, merge onto 50...... nothing. I had to go into second to get up to speed after traffic slowed. It just died. No noise or excitement. Nothing. Turns over super easy... no compression. Did a quick roadside test to confirm... 30 psi on #4. Call EricF. Go home. Towed it home last night w/ Isaac's brother's truck.
I'm going to start taking it out tonight and EricF and I are going to go get a new longblock tomorrow morning, hopefully.
Big thanks to Kevin, Isaac, Eric and Andres. They saved me big time. I haven't missed work because of the VW Andres is letting me borrow. Heres some other pics from my lovely Sunday:
http://nickflyman.com/volvo/volvo19/IMG_0145.JPG
http://nickflyman.com/volvo/volvo19/IMG_0148.JPG
http://nickflyman.com/volvo/volvo19/IMG_0155.JPG
Oh, the irony.
http://nickflyman.com/volvo/volvo19/IMG_0154.JPG
I drove home (Vero Beach, about an hour and a half from Orlando) on Saturday evening after work so I could attend my sisters birthday party on Sunday. So I made it home ok, no problems, ate dinner w/ my mom and then went over to kevin's (boosted) to hang out w/ him for a while. So we got kind of bored and decided to go for a ride in my car. Kevin drove it around a little, then we switched and I got in to drive. I made it to the end of second gear at full boost when I noticed something was wrong. I backed off and noticed while the motor was running on 3 cylinders. I figured I had probably blown an IC pipe off or something, so I pulled into a gas station to have a look. Popped the hood and we heard some horrific top end noise. Checked all the normal stuff, and everything seemed ok. Cranked it up again to try and diagnose the sound and thought it might be a shim that popped out of the bucket. Valve cover off.... nope. Cranked it up again to try and hear. This time, there was a terrible rattling noise, but the motor ran better....... hmmmm... At this point we were thinking valve seat, spring, bent valve; something in the head. Compression check showed 185 on 1, 2, and 3 but only 170 on 4. We drove to Sebastian, ripped the head off his old 245 and got some sleep.
Sunday morning I got up, went and ordered the HG set and we went over to the gas station where the car was. Pulled turbo/mani. Went to pull the intake and then we found it. Kevin reached into the intake port on #4 and pulled this gem out:
http://nickflyman.com/volvo/volvo19/IMG_0144.JPG
Yes, folks, thats 1/2 of a hose clamp. The other half had been chewed into the motor by the valve and was inside the cylinder. The only place I can figure this thing came from is the cold side of the IC. I got it from a garage where it had been sitting for some time under a bunch of crap. I inspected and flushed it out, so it must have been wedged solidly into the bottom. The amazing thing is that it stayed down there for a YEAR. I went to SE5 like this. Countless trips from Vero to Orlando. Strange. So we continue pulling the head off and finally have it removed to find this:
http://nickflyman.com/volvo/volvo19/IMG_0140.JPG
http://nickflyman.com/volvo/volvo19/IMG_0141.JPG
and this:
http://nickflyman.com/volvo/volvo19/IMG_0143.JPG
****.
We rolled the motor over and noticed that there was amazingly, no damage to the cylinder walls. The head was f-'ed and we knew that for a fact. This is the first time the motor had been opened up to my knowledge. There was still faint crosshatching on the cylinder walls (this is a 300+k mile motor!). The inside of the engine, except #4 obviously, was surprisingly in amazing shape. What a shame.
It was decided that I should clean the piston crown w/ emory cloth as best as possible, clean up the wagon head, and throw it all together in hope of just getting me back to Orlando where I can spend the time to do a motor swap.
http://nickflyman.com/volvo/volvo19/IMG_0149.JPG
We reassembled and got it running. Now the amazing thing is, that the motor ran very well. I drove it around Vero some, home that night, over to my sister's thing, and back home. The next morning (yesterday) I depart for Orlando. Fires right up, get on 95, no issues, pull off on 520, no issues, merge onto 50...... nothing. I had to go into second to get up to speed after traffic slowed. It just died. No noise or excitement. Nothing. Turns over super easy... no compression. Did a quick roadside test to confirm... 30 psi on #4. Call EricF. Go home. Towed it home last night w/ Isaac's brother's truck.
I'm going to start taking it out tonight and EricF and I are going to go get a new longblock tomorrow morning, hopefully.
Big thanks to Kevin, Isaac, Eric and Andres. They saved me big time. I haven't missed work because of the VW Andres is letting me borrow. Heres some other pics from my lovely Sunday:
http://nickflyman.com/volvo/volvo19/IMG_0145.JPG
http://nickflyman.com/volvo/volvo19/IMG_0148.JPG
http://nickflyman.com/volvo/volvo19/IMG_0155.JPG
Oh, the irony.
http://nickflyman.com/volvo/volvo19/IMG_0154.JPG