One end Fluro M16 rod ends, other side sized for poly (or stock rubber) bushings.
Radiused the bolt heads on the lathe, just because.
The Poly bushing side. Made the wall thickness of the shell 5mm. The stock ones were getting oval.. Seamless tubing used.
Bolts that were welded to them made from a weldable alloy (hot formed class 5.6). Thread length 60mm so I can adjust for all kinds of changes or modfy the rods (maybe for if i shorten trailing arms).
Primered. Rod ends LHD, bolts RHD. Adjustable when installed.
Spacers. Some high gloss paint too. And hopefully these rubber thingies keep the salt/water out. Added some grease to the inside of the covers.
Still need to properly adjust them but first impression is very good. Less slop in drive line (duh), less vibrations (old ones were stock, non adjustable), no noise, axle feels more planted, follows bumps in the road better, especially when road inclination changes (like sideways speed bumps, driveways). Driven about 200 Km now.
Still need to test high speeds and adjust them but the first short trips seem to be promising!
Got me this little digital angle gauge to check driveshaft alignment:
http://www.dx.com/nl/p/zndiy-bry-dx...WYy0CNPNvI9Q4IhoFCgAYaApHC8P8HAQ#.WHX7xlXhCpo
Nice little unit. Beats using the phone and destroying it in the process. Seems to work good. No changes in value after 24 hours stuck to the bed of my lil 6 ton lathe. Front is a bit flimsy, which is a shame, for the rest it is good value for $ (paid less elsewhere).
Only I managed to destroy the display back lighting. Must have dislodged a connection. Prob no warranty from the Chinese as usual so wil fix it myself.