![]() |
|
|
#601 |
|
JohnMc=500Dollar Mistake
![]() Join Date: Jan 2006
Location: Southern Maryland
|
That sucks
Something mechanical took a dump? |
|
|
|
|
|
#602 | |
|
Bluegrass/Celtic Junkie
Join Date: Jan 2005
Location: Richmond, VA
|
Quote:
__________________
66' 122 4dr (Project RAT ROD) /67' 122s (P132441M) / 88' 244DL / 86' 245GL all MTs of course EBAY Handle: Guitarphotoman Seller/Buyer feedback 1967 122s Restoration Thread |
|
|
|
|
|
|
#603 |
|
Board Member
Join Date: Jun 2004
Location: Houston, Texas
|
Dam.. 2jz then?lol j/k . HOPE TO HEAR MORE!
|
|
|
|
|
|
#604 | |
|
Home Schooled
Join Date: Nov 2008
Location: Portsmouth VA
|
i guess youll just have to try again right?
__________________
Quote:
build thread; http://forums.turbobricks.com/showthread.php?t=251729 '92 244. 601 red, stock, awesome. http://forums.turbobricks.com/showth...48#post4123948 '86 245. Dead, gone '88 780. DUI'd and on the way out. '82 244. dead and gone
|
|
|
|
|
|
|
#605 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
After the valve to piston matchup, were ready for business again..
![]() ![]()
__________________
![]() 89 244tic- Ultimate sleeper - MZR/Duratec 2.3, Eagle rods, CP 8.5:1 jugs, GT3071R , 5R55E, Home-made turbo and intake manifolds, Electromotive TEC-GT, Tial BOV and WG, PCS Paddle shifters, Electronic gear select module 93 965- Daily driver 91 944se- Resto project 66 122s- Stock Last edited by TerribleOne; 11-04-2012 at 10:03 PM.. |
|
|
|
|
|
#606 |
|
Board Member
Join Date: Jun 2008
Location: tir porthladd triphlyg
|
What's that dragster minivan doing?
__________________
cassie wuz here, stealin ur giant sigz |
|
|
|
|
|
#607 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
![]() Guess what? It's broken again. I've been fighting valvetrain issues for the past few months.. Haven't really had time to work on it every day, but today I finally tore into it and found the variable valve timing actuator to be faulty which is what's been giving me all the excessive valve train noise. Still haven't made the decision to ditch it or just get a modified actuator with hardened stop pins etc.. Should have a new turbo in soon and possibly new injectors. The drag car is in hibernation.. It'll be out next spring for a good shakedown, I'll add more details about it later. |
|
|
|
|
|
#608 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
It runs again, and quite well too.. Figured out how the VVT wasn't getting oil and I've got a new turbo on order.
![]() |
|
|
|
|
|
#609 |
|
Board Member
Join Date: Sep 2004
Location: Illinois
|
What turbo you gettin' this time??
__________________
Joe Bieda V.C.O.A. Midwest Chapter President. 1984 242 M46 GLT. -Couple of things done to it ![]() 1998 S70 Auto. -LONG history. 1983 242 M46 Check out http://JJFAB.net For your K24 CBV blanking plates and oil feed/return flanges!! |
|
|
|
|
|
#610 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
Gt3071r
|
|
|
|
|
|
#611 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
Quick Video clip on wastegate spring only.. 11psi
|
|
|
|
|
|
#612 |
|
Turbonormalizer
![]() Join Date: May 2003
Location: Kubotaville Va.
|
New turbo is almost ready to go on..
![]() |
|
|
|
![]() |
| Thread Tools | |
| Display Modes | |
|
|